| date
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place
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process
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| November 22, 2002
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Tihange Nuclear Power Plant , Tihange , Belgium
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On November 22, 2002, an incident occurred in Block 2 ( INES 2). Although the reactor was shut down at this time and was no longer critical, it was still producing heat due to the decay , which, as in power mode , is dissipated by the circulation of the coolant in the primary circuit . As a result of a test, a safety valve on the pressure regulator was opened by mistake , as a result of which the pressure in the primary circuit fell from 155 bar to 85 bar in a very short time . The high pressure in the primary circuit during operation causes the water does not boil even at a high temperature, but in the liquid aggregate state remains. However, if the pressure drops, the boiling temperature of the water decreases and it changes to the gaseous state. Then the decay heat of the fuel assemblies can no longer be removed and there is a risk of a core meltdown . In this case, however, several safety systems were activated due to the rapid drop in pressure, which fed water into the reactor and thus further cooled the fuel assemblies. The incorrectly opened pressure relief valve was only closed again after three minutes due to communication problems.
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| April 10, 2003
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Paks Nuclear Power Plant , Paks , Hungary
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When cleaning fuel rods in Unit 2, the cladding of 30 fuel assemblies was damaged, which almost triggered a chain reaction. Radioactive gas escaped. The measuring probes in the area registered noble gas pollution above the limit values . The reactor stood still until the beginning of 2005, the damage totaled around 200 million euros.
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| 2003
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Kozloduy 3 nuclear power plant , Kozloduy , Bulgaria
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In full load operation, a primary circuit leak suddenly occurred at a weld seam. The emergency cooling started working. In contrast to the more powerful Units 5 and 6 and all western pressurized water reactors, units 1 to 4, which have now been shut down, were able to shut off individual segments of the primary circuit with valves. A shut-off was made so that the water loss could be stopped after a relatively short time.
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| 2004
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Vandellòs 2 nuclear power plant , Vandellòs , Spain
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The supervisory authority CSN established that the operator of this plant had kept a line corrosion from it for years, which could have called the functionality of the component cooling into question. If the two lines had failed at about the same time (and not just one, as happened), the reactor would hardly have been able to be cooled down (INES 2)
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| November 4, 2004
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Balakovo Nuclear Power Plant , Balakovo , Russia
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An incident occurred in Balakovo. The reactor was shut down. According to the operator Rosenergoatom , no radioactivity escaped.
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| 2005
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All NPPs, France
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The ASN supervisory authority announced that - in the event of a leak in the reactor circuit - if the line suction strainers of the emergency cooling in the containment sump (with waste such as insulating material or rags) were blocked, "the core cannot be cooled". INES classification: 2. Improvement measures have been announced. The cleanliness is the smaller problem; the aforementioned insulating material only comes off due to a leak that has occurred, due to the pressure forces of the exiting water jet.
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| March 28, 2005
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Leibstadt nuclear power plant , Leibstadt , Switzerland
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The Leibstadt nuclear power plant came to a standstill for five months on March 28, 2005. The reason for this was damage to the generator; the repair work on the generator was not the responsibility of the HSK (nuclear supervisory authority), since the nuclear part of the nuclear power plant was not affected.
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| April 20, 2005
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Sellafield , UK
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On April 20, 2005, a leak in a line carrying highly radioactive fluid was discovered at the Thermal Oxide Reprocessing Plant . A total of 83 m³ of liquid leaked to the bottom of the chamber, including 22 t of nuclear fuel (mainly uranium with around 160 kg of plutonium). The leak was only discovered after eight months due to a malfunction of the level meter in the sump of the chamber and failure to heed alarm signals. The removal of uranium-contaminated samples that indicated a leak did not lead to any reaction. With proper treatment of the problem, the leak could have been detected as early as August 28, 2004. The leaked liquid was caught by the stainless steel-clad floor of the chamber and later removed with the built-in sump pumps. Neither workers nor the population were harmed in the incident, it was classified at INES Level 3.
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| June 29, 2005
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Forsmark , Sweden
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On June 29, 2005, radioactive water from the interim storage facility for low and medium- level radioactive waste in the Swedish Forsmark nuclear power plant entered the Baltic Sea. Ten times the normal level of radioactive cesium was measured in the waters near the power station. According to the Swedish radiation protection institute SSI, however, this is still within the permissible limits. Corroded tin containers with radioactive waste were probably to blame for the leak.
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| March 1, 2006
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Kozloduy 5, Bulgaria
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During the shutdown of the 5th block on March 1st after a main coolant pump failed, a third of all controls were stuck in the upper position. An emergency boration had to be carried out to shut down the reactor . The operator originally classified the incident at INES Level 0 , but the regulatory authority corrected it to Level 2 .
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| July 25, 2006
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Forsmark , Sweden
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On July 25, 2006, the Forsmark-1 reactor was automatically disconnected from the power supply after a short circuit in the substation through which the nuclear power plant transfers its electricity to the general grid. This led to a load shedding of the generator and the heat produced in the reactor could no longer be converted into electrical power. The reactor was shut down via an emergency shutdown . The electricity for the control of the nuclear power plant and the feed pumps , which have to dissipate the decay heat, failed. Alternatively, it had to be provided by diesel emergency power generators . However, two of the four generators could not feed into the emergency power grid because they remained electrically connected to the 500 V line, which had failed. In addition, the power supply for some of the measuring devices in the control room failed . After 23 minutes, the other two diesel generators could be switched on manually. This connection enabled the water level in the reactor to be raised to normal again. According to the Swedish radiation protection authority SKI, an acute core meltdown was not to be expected at any time of the incident, but it would have been a very serious incident.
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| 2007
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Leibstadt, Switzerland
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When the automatic pressure relief system (DAS) was accidentally triggered during a test in normal operation, some valves for the pressure relief of the reactor system opened. The water had to be replenished with the emergency cooling .
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| 2007
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Dampierre Nuclear Power Plant , Dampierre-en-Burly , France
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A similar incident as in Forsmark: failure of the external network including the reserve network as well as an emergency diesel generator with 100% supply capacity. The factory is about 80 km from Paris. The reactor was cooled down with the only remaining diesel (100%). Nevertheless, the French authority ASN only rated the incident as INES 1. Reason: The redundancy reserves of the self-steam driven auxiliary turbine (ready for immediate use) and the gas turbine (whose synchronization could take hours) were still available.
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| 2007
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Penly 2 Nuclear Power Plant , Penly , France
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When the block was restarted after the overhaul in April, after two days of testing, it was noticed that all emergency cooling pumps would have been unavailable during the two days if required.
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| 2007
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Cattenom Nuclear Power Plant , Cattenom , France
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The plant on the border with Saarland released zinc into the Moselle in June in a concentration that was above the permitted limit. The annual limit has not been exceeded, writes EDF; it remains unclear whether it was normal zinc ( heavy metal ) or the radioactive isotope .
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| August 21, 2007
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Beznau 1 nuclear power plant , Beznau , Switzerland
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On August 21, Block 2 was undergoing annual overhaul. The common reserve grid feed was switched off for maintenance work. To compensate, the emergency diesel generator of Block 1, which is running at full load, was switched on while idling. After the reserve network was restored, it was noticed that this diesel would not have fulfilled its emergency power function due to a malfunction. According to the HSK authority, there would theoretically have been a cross connection to the emergency diesel of the shutdown unit 2, but this diesel was also in maintenance. If a flood had set in like just twelve days before, the hydropower plant would not have been available with enough emergency power either. With an additional interruption of the main network, KKB 1 would only have two diesel generators left to prevent the core meltdown, each with only 50% of the required emergency power output. These or the emergency cooling pumps connected to them could possibly fail relatively quickly after being switched on due to a fault.
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| 2007
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Vandellòs 2 nuclear power plant , Spain
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After the eight Spanish NPP units had recorded 14 INES incidents in just three consecutive months, a similar incident occurred in Vandellos in December, as described above under Leibstadt. During a test with the reactor running, some shutdown rods unexpectedly collapsed into the core. According to the supervisory authority CSN, this led to a pressure drop in the reactor circuit, and thus to the triggering of the emergency cooling. The pressure build-up that followed led to the activation of the reactor safety valves and the leakage of slightly contaminated cooling water into the containment sump. An internal emergency pre-alarm was triggered.
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| 2008
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Paluel Nuclear Power Plant , Paluel , France
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Incorrect dispositions of insulation fittings were found in one of the four blocks in February, which had existed for more than five months. “This questioned the tightness of the containment,” writes the ASN, “during the period in question had an accident happened”. A core melt could have resulted in releases.
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| February 2008
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La Hague, France
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The highly active substances treated in this reprocessing plant continuously release explosive hydrogen which, when reacting with oxygen , threatens the building's tightness, which is much more vulnerable than in western nuclear power plants. To avoid an explosion, the building air is freed of hydrogen by continuous circulation. For 3.5 hours this circulation only worked in normal operation, both reserve air lines were not operational due to defects or maintenance work.
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| April 2008
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Ascó Nuclear Power Plant , Ascó , Spain
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Discovery of radioactivity from the fuel assembly building on the factory premises. Although the doses were below the limit values, the CSN authority classified the incident with INES 2: The operator had misinterpreted clear indications (triggering activity alarms) for months and most recently provided the CSN with downplaying data.
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| April 2008
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Flamanville Nuclear Power Plant , Flamanville , France
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In block 2, according to The ASN supervisory authority found "severe corrosion" in the engine cooling lines of both emergency diesel generators. The safety reserves for an emergency power supply were therefore small.
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| May 2008
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Cruas 4 nuclear power plant , Cruas , France
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This block was at a standstill with the reactor open. Suddenly it was noticed that two valves of the residual heat removal were only partially open for a full four days, which significantly impeded the post-decay heat removal. ASN does not write anything about an automatic alarm, so it is conceivable that after these four days the whole thing was only noticed by steam phenomena in the reactor flood basin (Note: NPPs must cool the fuel even after the first cooling and opening of the reactor, since the fission products continue to decay with decreasing intensity). The fact that no unusual doses were apparently registered can be explained by the fact that the reactor water is technically cleaned before it is shut down.
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| June 2008
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Rivne Nuclear Power Plant , Rivne , Ukraine
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Almost two weeks after Krško, the same scenario was repeated in the Ukrainian nuclear power plant Rivne / Rowno. This time the media reported very little or not at all. The power plant was temporarily taken off the grid.
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| July 8, 2008
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Eurodif , France
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On July 8, 30 cubic meters of radioactive liquid leaked from the Eurodif uranium enrichment plant and some of it got into the surrounding rivers.
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| July 23, 2008
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Tricastin Nuclear Power Plant , Pierrelatte , France
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Around 100 people were radioactively contaminated during maintenance work in the power plant, but below the dose limits
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| August 15, 2008
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Santa María de Garoña, Spain
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On July 15 and August 19, the plant's two battery systems were tested. According to the CSN authorities, the capacity they have determined was insufficient. In the event of a malfunction, these direct current systems fulfill various safety functions, for example as a starting aid for the emergency diesel or display of the reactor status. The main problem with this event is that after the malfunction of the first system was discovered on July 15, the operator did not test the second system immediately, but rather on August 19.
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| August 25, 2008
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Fleurus , Belgium
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In the field of waste disposal at the Institute for Radionuclides (French: Institut des Radioéléments (IRE) ) in Fleurus, Belgium, an estimated 45 GBq of iodine-131 was released via the chimney when liquid waste was transferred. The Belgian nuclear regulatory authority Agence Fédérale de Contrôle Nucleaire (AFCN) shut down the IRE, a producer of radioisotopes for the medical sector, immediately after the accident was reported. Six days after the incident, the police warned the residents about the consumption of fruit, vegetables, milk and water from the area via loudspeakers after the government's crisis team revoked the initial all-clear and activated the European information system ECURIE . The event was classified as a “Serious Incident” at level 3 on the INES scale.
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| October 2008
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Gravelines 5 Nuclear Power Plant , Gravelines , France
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During the revision in June, the engine of one of the two emergency diesel engines was replaced. It was only after more than three months, in October, that it was discovered that this replacement engine had not been properly installed: The diesel would not have been available for three months, which represents a redundancy failure that was far too long.
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| September 5 to November 6, 2008
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Ascó , Spain
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Between September 5 and November 6, eight INES incidents were registered in the double-unit facility, five of them in Unit II.
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| 2009
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Cadarache , France
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In the French nuclear facility Cadarache, 39 kilograms of plutonium were probably discovered as early as June during dismantling work. The nuclear safety agency stopped work on October 15 and classified the incident in INES category 2. In addition, they accused the operator of not having reported the event in time.
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| December 2, 2009
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Cruas Nuclear Power Plant , Cruas , France
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On December 2, in Block 4 of the Cruas nuclear power plant, leaves and other autumn debris collected in the river's cooling water circuit and blocked it. The reactor was switched off and switched to hot standby with the flow-independent emergency feed via the steam generator . However, even after this process, the reactor core must be cooled further with the river cooling water - because of the ongoing decay - in the so-called post - cooling operation so that it does not overheat and melt. The internal emergency plan was triggered and, as an emergency measure, the cooling pool cooling circuit for the spent fuel elements was connected to the reactor cooling circuit. After 5.5 hours, the blockage in the intake structure was cleared and normal after-cooling operation was restored. The incident was classified as INES 2.
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| December 27, 2009
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Fessenheim Nuclear Power Plant , Fessenheim , France
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On December 27, a similar disruption occurred in the Fessenheim nuclear power plant as in Cruas, where plant residues got into the cooling circuit when the reactor was started up (INES 1).
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